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A mechanic manually rotating a Chevy small-block engine with a degree wheel for precise camshaft timing adjustments
The Fix
Resurrecting a Near-Dead Small-Block Chevy
BY Jeff SmithImages BY THE AUTHOR
N

early all performance automotive magazine stories take the positive approach. We bolt on the parts, the engine makes more power, and the paintjob comes out perfect every time. Everybody wins, the birds sing, and life is grand. But that’s rarely how it works in the real world.

This story begins with gritty facts that unfortunately happen all too often. The owner of the engine in question has requested to remain anonymous mainly because he now feels like he’s been ripped off. It all started when he asked if we could spend a few minutes curing an ignition problem.

The engine in question was not a typical mild street small-block but instead a high-compression street/race small-block Chevy that was aimed at attacking the local eighth-mile dragstrip.

The 403ci small-block was underperforming, and the timing numbers on the balancer bounced around badly at idle; when revved, the numbers instantly retarded between 15 and 20 degrees. At first it appeared that this mechanical roller-cammed engine was suffering from a missing cam button. This allows the distributor gear to push the cam forward in the block, retarding the ignition timing as the rpm increases.

This seemed odd but very little facts were known because the original engine builder had died. Engine details were foggy but the seller claimed it was a 403ci with 13.5:1 compression, a big mechanical roller cam of unknown specs, and good iron 215cc Dart heads. We removed the valve covers to find a Coleman stud girdle and big dual valvesprings.

When we pulled the front timing chain cover, we were surprised to find a Comp roller cam button. Closer inspection revealed that the cam gear protruded from the block roughly 1/4 inch, which radically misaligned the chain to the crank gear. Before disassembly we also checked the cold lash and found it ranging wildly from 0.020 to 0.032 inch!

We decided to pull the engine out of the car. With the intake removed we were greeted with an Isky rev kit. For readers not familiar with that term, it was once common to outfit big roller cams with springs between the cylinder head and each mechanical roller lifter.

We decided to yank the cylinder heads to remove the rev kit and discovered all kinds of problems. The original builder used stock head bolts that were under-torqued or had relaxed. We also noticed the head gasket was close to failing between the center cylinders where the heat concentrates on small-blocks.

Worse yet, the head gaskets were for a 4.00-inch bore 350 engine that placed the fire ring into the cylinder. Not good. We also measured the cylinder and combustion chamber volumes and discovered the compression was actually 12.13:1 (see sidebar).

The main issue however was still the improper alignment of the cam and crank timing gears. After we removed the heads, it was clear that the cam was pushed forward because the rear cam plug had been installed too deeply. After thinking about how this blunder could have occurred, we think that someone installed the cam plug in the back of the block at the very last and drove it in too far, forcing the cam (with the cam button) forward, bending the stock timing cover. We used a rubber mallet on our camshaft installation tool to drive the cam (and rear plug) backward until the cam face was flush with the front of the block.

We then ran through the process of finding the cam’s opening and closing points at 0.050-inch lobe lift, which gave us duration on the intake and exhaust. It’s possible the numbers are not 100 percent accurate but they are close enough to give us an idea of the size of the cam. A Summit online cam program crunched the numbers for us and produced 254 degrees of intake duration at 0.050-inch lobe lift with 258 degrees on the exhaust and roughly 0.610-inch valve lift at zero lash using light checking springs.

We decided to retain the camshaft but to replace the rev kit lifters with more modern Comp Cams mechanical roller lifters. We checked the net valve lift with the new lifters, the big springs, new Comp pushrods, and ARP rocker studs with the stud girdle in place with 0.020 inch of cold lash. This produced a max valve lift at a lower 0.570 inch. Part of this change in lift includes the 0.020 inch of lash along with roughly 0.020 inch of valvetrain deflection from the high spring pressure.

We also installed checking springs on Number One cylinder and checked the valve-to-piston (V to P) clearance. The intake side was too close at 0.070 inch while the exhaust enjoyed more room at around 0.140 inch at zero lash.

To improve the intake V to P we retarded the cam 4 degrees with the Cloyes crank gear, which added intake P to V clearance but also tightened up the exhaust side with 0.120 inch for both the intake and exhaust. We finished up with a new Cloyes aluminum cover that allowed us to easily set cam endplay.

While disassembling the heads to check the valvespring pressure, we discovered several broken valve locks. We replaced them all with new Comp 10-degree locks. This damage probably occurred when the engine was revved to 7,500 rpm on several occasions. We informed the new owner that we felt this engine should now not spin past 6,500 until we have some time on the engine to establish if the valvetrain is stable. We also checked TDC on the balancer and found it off by about 2 degrees, so we changed the zero mark on the balancer and marked a new location for 36 degrees total advance.

After we ran the engine on our Summit Racing test stand, we delivered it to Tom Kirchhoff’s Performance Auto in Waterloo, Iowa, to run on their Stuska dyno to produce some actual power numbers. We really didn’t expect too much from this small-block, but we were hoping to see 520 lb-ft of torque and 550 hp.

Dyno day was disappointing but not unexpected. After setting the timing at an indicated 36 degrees, the engine ran well using Sunoco 110 race gas. The 403 managed to pump out an encouraging 528 lb-ft of torque at peak at 4,800 rpm but could only manage 519 hp at 5,900. Revving past 6,000 rpm pushed the engine into what appeared to be serious valve float, and the power numbers plummeted. We agreed with dyno operator Curt Wollin who suggested that it would probably be best to stop running the engine until we fixed this problem.

The dyno curve also revealed a serious dip in the torque curve that indicated to us a loss of valve control prior to the peak horsepower point. The solution to this problem was to dial in a different, shorter duration mechanical roller cam.

At least that’s what we thought would solve the problem. But it turned out we were wrong.

We went back to the shop, disassembled the engine and removed the original mystery cam. The cam we chose was selected out of expediency—we had one sitting on the shelf. The cam chart will give you the details, but the short version is that it was 12 degrees shorter in duration on the intake side and 10 degrees on the exhaust with slightly less lift. We also put it in at 108-degree intake centerline instead of 106 thinking that would help the top-end power.

We reused the lifters, pushrods, rockers, and valvesprings after closely inspecting the locks to make sure none had been damaged. All looked good. With everything buttoned back up, we also decided to change to a different intake. We dumped the original single plane in favor of a Holley Strip Dominator. In previous testing we found this Holley manifold is both affordable and generally better at peak horsepower and average torque than most other single-plane intakes. We retained the original 850-cfm Holley Street HP carburetor.

We began the second dyno day with much anticipation because we thought we now had control over the valvetrain. We expected the peak torque numbers to be substantially better than the previous test’s 527 lb-ft peak number.

That didn’t happen.

Instead, the engine suffered a massive loss of both torque and horsepower. The first pull barely made 480 hp at 6,000 rpm and the torque was off by 60 lb-ft. If that wasn’t bad enough, the dip in the power curve remained. Something was seriously wrong.

We had set the ignition timing at 36 degrees so Wollin suggested we add more timing. We added 4 degrees and the power jumped dramatically. We added another 4 degrees and power improved again. The timing indicated on the balancer was 44 degrees BTDC, which was clearly not accurate. We inspected the spark plugs and noted that the color on the ground strap revealed the timing was close to optimal.

We then tried adding a 1.5-inch Wilson carb spacer between the Holley manifold and the 850 carburetor and this helped slightly with a gain of roughly 4 to 5 hp through most of the entire curve. However, the torque curve still exhibited a slight depression at 4,700 rpm that we were never able to eliminate. At least now the engine was positively responding to changes.

Wollin had yet another recommendation. His experience on big-piston dome engines revealed they responded to using non-projected nose spark plugs. Our engine was fitted with projected nose plugs, so this was an easy change. The engine improved again by an average of 4 lb-ft of torque throughout the entire curve and produced 525 for peak horsepower at 6,400 rpm with a peak torque of 515 lb-ft at 4,900.

These are similar numbers to our first test but a comparison of the torque curve from the big-cam test versus this second small-cam test revealed that we lost torque with the smaller camshaft. Wollin suggested that we go back to the original cam to improve the overall power. Now that we know that the first test suffered from retarded ignition timing, the larger cam would obviously now make a bunch more power.

With 44 degrees showing on the balancer, it was clear that the harmonic balancer outer ring had slipped. We had checked the location of top dead center (TDC or 0 degrees on the balancer) before the first test session and found it was off by 2 degrees, which we assumed was only a minor error.

After returning to our shop, we checked TDC again and we found the outer ring of the balancer had moved by 7 degrees. So just within the dozen or so pulls on the dyno, the balancer ring had moved an additional 5 degrees! This means that while the indicated timing was at 44 degrees, the true timing was only 37 degrees BTDC. We started the first dyno session with the big cam with probably only 30 to 31 degrees of total timing and that was why the engine performed so poorly.

We will now replace the harmonic balancer with a new SFI unit and double check our TDC mark again to ensure that the ignition timing indicated on the balancer is absolutely correct.

Our big mistake was not adding ignition timing to the engine on the first dyno session. Had we tried that we might have realized the harmonic balancer was not accurate and the engine would have certainly made much more power. The first session made only 519 hp at 5,900 because the late ignition timing was holding it back. We’re fairly certain this engine can make 540 to 550 hp with the bigger camshaft combined with proper ignition timing.

The error of not adding more ignition timing in the first dyno session was based on our concern that the valvetrain was in distress and it might drop a valve because of the broken valve locks we had found.

If this was a made-for-TV movie, we would run the engine one more time with the bigger cam and make hero power. But that’s not going to happen because the owner has already spent over $1,000 on testing. Sure, it would be nice to know but sometimes the realities of blue-collar finances muscle their way into the conclusion of a good story.

Overall, we did radically improve this small-block’s power and reliability. The two biggest issues we repaired were the cam shoved too far forward and the demonic harmonic balancer. The plan now is to reinstall the original camshaft, re-verify P to V clearance, and stuff the engine back in the car so the owner can put all his newfound power to use. This process took much longer than it should have to uncover this small-block’s flaws and it seemed like a battle the entire way.

This was a little like a detective story where the mechanical sleuths had to root out all the clues, find the culprits, and put them away. As usual, it was a learning experience and hopefully what we discovered can be put to use the next time you’re faced with a similar situation. Let’s just hope you uncover your problems much quicker than we did.

Calculating Compression Ratio
Given all the issues with this engine, we decided to verify the compression ratio since the dome did not look sufficient to support the claimed 13.5:1 compression. We measured the combustion chamber at 62 cc. With a 4.135-inch bore, we theoretically positioned the piston at 0.200-inch below the deck and calculated the pure flat top piston cylinder volume at 2.685 ci. We then converted that to cc by multiplying 2.685 ci by 16.3871, which gave us 43.99 cc, which rounds up to 44 cc.

We then measured the actual cylinder volume again placing the piston 0.200-inch down in the cylinder. This produced 45 cc, which is 1 cc larger than our calculated cylinder volume. Even though the piston has a dome, it also sports very deep valve reliefs, which essentially offset the dome volume. The result is something very close to a pure flat-top piston with a 1 cc valve relief.

We used these numbers to calculate the compression ratio with a 4.135-inch bore, a 3.75-inch stroke, a 62cc chamber, a piston with the equivalent of a 1cc valve relief, a 0.010-inch deck height, and a compressed head gasket thickness of 0.041 inch. The combination of a 0.010-inch deck height and a 0.041 gasket pushes the quench to 0.052 inch, which is quite wide and further lowers the compression. All these factors combine to produce a 12.13:1 compression ratio.

Cam Specs chart
Parts List chart
The lifter valley of a disassembled Chevy small-block engine showing cleaned cylinder walls and exposed valve springs
1. Once we removed the intake, we discovered this old-school Isky rev kit with springs over the lifters to help control the lifters. We eventually removed this system and changed the lifters.
Close-up of a Chevy small-block engine's front face, highlighting the camshaft retainer and freshly machined surface
2. The initial culprit for our ignition timing problem was the cam was pushed forward because the rear cam plug was installed too deeply. We’ve illustrated this with a different small-block because we forgot to shoot the photo before we pushed the cam plug back into its proper position. We think this occurred after the timing cover was installed.
Set of valve locks removed from a Chevy small block during engine repair
3. While removing the springs to check installed height, we found several broken valve locks. This was probably caused by the earlier over-rev. Frankly, the owner is incredibly lucky these broken locks didn’t drop a valve and destroy the engine. Circular wear marks on the surviving locks were a clue that the retainers were losing their grip on the locks, allowing the retainers to spin. This is a classic indication that the valvetrain was out of control.
Combustion chambers of a Chevy small-block engine with pistons and head gaskets prepped for installation
4. The piston domes were rather small for the claimed 13.5:1 compression. Actual compression checked out at 12.12:1. We also added ARP studs to the engine to offer a better chance of keeping all that cylinder pressure inside the cylinders where it belongs.
A valve spring pressure tester displaying a spring load reading of 598.4 pounds, ensuring proper performance specifications
5. We checked the dual valvesprings for load and found 260 pounds on the seat at 1.800-inch installed height and slightly more than 600 pounds at 0.600-inch lift.
An overhead view of the Chevy small-block lifter gallery, showcasing pushrods and lifters set in alignment
6. We replaced the rev kit roller lifters with a new set of Comp Endure-X mechanical roller lifters along with a set of proper length Comp 0.080-inch wall pushrods.
A mechanic lubricating a camshaft for installation into a Chevy small-block engine during a rebuild process
7. After the first dyno test that did not go well, we returned to the shop, pulled the old cam because we thought the engine was in valvetrain distress. This new Comp mechanical cam offered 12 degrees shorter duration and less lift, which turned out to not be a good idea.
A Chevy small-block engine fitted with a Cloyes timing cover, showing precise alignment and timing setup tools in use
8. With the cam in place, we set the cam endplay with the Cloyes cover. This cover makes setting the roller cam endplay really easy.
Installing valve covers on a rebuilt Chevy small block engine
9. We also suspected that the no-name intake manifold was less than optimal, so we bolted on a Holley Strip Dominator intake, which is slightly taller and should make a little more peak torque and horsepower. We could afford to add a taller intake since the engine is in a 1955 Chevy, which has a very deep engine compartment.
Chevy small block engine on a dyno setup for testing and tuning
10. After several sessions on Performance Auto’s dyno, we discovered that the timing mark on the balancer was in error. This photo was taken before we added the Wilson carb spacer.
Close-up of hydraulic lifter from a Chevy small block engine
11. The first pulls in session two were horribly down on power. Once we realized we couldn’t trust the timing mark on the balancer, we then relied on the heat color on the ground strap as an indicator of ignition timing. With the heat mark roughly in the middle of the ground strap, we decided the timing was close to optimal.
Comparison of new and used spark plugs for Chevy small block maintenance
12. Curt Wollin suggested replacing the projected nose spark plugs (right) with a non-projected nose spark plug (left). The theory is that the projected snout places the working end of the plug too close to the piston dome, which inhibits the flame front. The non-projected nose plugs boosted the power an average of 4 hp throughout the entire test.
Timing mark alignment on the Chevy small block harmonic balancer
13. This is a photo of the TDC test performed after the second dyno session. The notched yellow mark is not the original TDC. Our first test placed TDC at the large white mark. After the second dyno session, we checked TDC again and TDC moved to the zero mark on the blue tape (arrow). This means TDC moved roughly 7 (closer to 8) degrees from the original white mark. Each time we ran the engine through a test on the dyno it appears the ring was moving. Clearly the harmonic balancer was failing. We will replace it with a new SFI-rated balancer.
Installing a spacer plate on the intake manifold of a Chevy small block engine
14. This 1.50-inch-tall Wilson carb spacer was also worth 4 to 5 hp over most of the power curve. If we had not been distracted by the ignition timing fiasco, we could probably have made even more power by optimizing jetting, lash, and other changes.
DYNOtest
15. This graph combines the original torque and horsepower curves (TQ1 and HP1) with the new test (TQ2 and HP2). TQ2 is down 20 lb-ft at 4,700 rpm and that dip is something as yet unexplained. But it is obvious that the longer duration cam made more torque even at this low rpm (with less than ideal ignition timing!), so we will go back to the bigger cam for the final configuration. The second session eventually increased peak power after adding the necessary ignition timing. We think the bigger cam with proper ignition timing should net 540 to 550 hp. Whew!
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